Don Patrick
Well Known Member
Hello everyone,
I have a legacy D180 with the HS34 and the SV32 roll and pitch servos. Out of the blue, the roll servo will go on and offline. I have double checked the connections for all the wires. When I’m on the ground, the servo calibration is perfect along with the test.
I moved my Uavionex tail beacon from the tail to the right wing tip, where it is embedded inside the wing tip. The shielded wires for that unit occupy the same conduit as the SV32. Is it possible that this could be causing the intermittency?
I haven’t flown it with the tailbeacon turned off, but that is the next test. If that is the cause, is there a solution without moving the tail beacon from that location?
Thanks
Don
I have a legacy D180 with the HS34 and the SV32 roll and pitch servos. Out of the blue, the roll servo will go on and offline. I have double checked the connections for all the wires. When I’m on the ground, the servo calibration is perfect along with the test.
I moved my Uavionex tail beacon from the tail to the right wing tip, where it is embedded inside the wing tip. The shielded wires for that unit occupy the same conduit as the SV32. Is it possible that this could be causing the intermittency?
I haven’t flown it with the tailbeacon turned off, but that is the next test. If that is the cause, is there a solution without moving the tail beacon from that location?
Thanks
Don