Gents,
I am completing the drilling process on my RV-7A gear and I am rather frustrated.
I followed the directions to drill the axle nut and wasn't pleased with the outcome.
Here is what I did.
I installed the wheel and tightened the nut the appropriate amount. I used a transfer punch in the 1/8" holes in the nut to mark the axle. I ran a #40 long drill to cut a little of the thread so that the nut could be easily removed. I then removed the nut and wheel. The nut came off with some resistance and small aluminum thread shaving were removed in the process. I used my drill press to drill each side on the axle for the cotter pin hole.
When I installed the wheel and nut I had a misalignment with one of the holes in the axel. Slightly off in rotation and off along the axle axis. This was caused by the fact that drilling holes in treads isn?t exact. So to fix this problem I decided to use a small round file and slot the hole in the axel. After filing for a while I was able to finally get the cotter pin in. It definitely fought me all the way.
I know where I made my mistake so I decided to try another approach on the other gear leg. This time I only marked one side with the transfer punch and drill, removed the wheel/nut (I needed to use a large wrench to get the nut off-deformed threads) and drilled only one side with the drill press. Then I installed the nut and inserted a 1/8 rivet into the nut/hole to pin the nut in position on the axle. I went back to the drill press and using the nut hole as a guide drilled the remaining hole in the axle. This method worked well except the original hole shifted slightly along the axle axis and when the nut is tightened down the holes don't align as they should. When they do align I do not get the preload I had intended. So I have too much slop (not enough preload) when the nut is installed and the cotter pin is in place.
This has been a frustrating day.
I am considering drilling a second cotter pin hole in the first gear leg using the method I used on the second gear leg but I hate to have extra hole in my project. As far as not having enough preload, I can do a few things. First I can make a new axle spacer that is wider then the supplied unit or purchase axle shims or I can order a new nut and maybe it will work well.
If after drilling the holes the nut can not be tightened down enough to get the holes aligned there is a rather easy fix for that. Just sand down the face of the nut until the holes align (material removal). If on the other hand you need to add material (that is my case) the solution is a little more involved.
It sure would be nice to have slots in the nuts instead of holes (future business opportunity?) sort of like a castle nut. That would make things much easier.
I wanted some input (opinions) on the next steps.
Thanks,
Paul
RV-7A (Finishing Kit)
I am completing the drilling process on my RV-7A gear and I am rather frustrated.
I followed the directions to drill the axle nut and wasn't pleased with the outcome.
Here is what I did.
I installed the wheel and tightened the nut the appropriate amount. I used a transfer punch in the 1/8" holes in the nut to mark the axle. I ran a #40 long drill to cut a little of the thread so that the nut could be easily removed. I then removed the nut and wheel. The nut came off with some resistance and small aluminum thread shaving were removed in the process. I used my drill press to drill each side on the axle for the cotter pin hole.
When I installed the wheel and nut I had a misalignment with one of the holes in the axel. Slightly off in rotation and off along the axle axis. This was caused by the fact that drilling holes in treads isn?t exact. So to fix this problem I decided to use a small round file and slot the hole in the axel. After filing for a while I was able to finally get the cotter pin in. It definitely fought me all the way.
I know where I made my mistake so I decided to try another approach on the other gear leg. This time I only marked one side with the transfer punch and drill, removed the wheel/nut (I needed to use a large wrench to get the nut off-deformed threads) and drilled only one side with the drill press. Then I installed the nut and inserted a 1/8 rivet into the nut/hole to pin the nut in position on the axle. I went back to the drill press and using the nut hole as a guide drilled the remaining hole in the axle. This method worked well except the original hole shifted slightly along the axle axis and when the nut is tightened down the holes don't align as they should. When they do align I do not get the preload I had intended. So I have too much slop (not enough preload) when the nut is installed and the cotter pin is in place.
This has been a frustrating day.
I am considering drilling a second cotter pin hole in the first gear leg using the method I used on the second gear leg but I hate to have extra hole in my project. As far as not having enough preload, I can do a few things. First I can make a new axle spacer that is wider then the supplied unit or purchase axle shims or I can order a new nut and maybe it will work well.
If after drilling the holes the nut can not be tightened down enough to get the holes aligned there is a rather easy fix for that. Just sand down the face of the nut until the holes align (material removal). If on the other hand you need to add material (that is my case) the solution is a little more involved.
It sure would be nice to have slots in the nuts instead of holes (future business opportunity?) sort of like a castle nut. That would make things much easier.
I wanted some input (opinions) on the next steps.
Thanks,
Paul
RV-7A (Finishing Kit)